Turbonic
Member
Had the inevitable blown PCV check valve in my intake manifold and prior to that my purge solenoid went out. I've already replaced the other two PCV check valves. I replaced the purge solenoid and installed the PCV bypass/fix kit and at the same time installed a boost/vacuum gauge and AFR gauge. Car runs better than it ever has before, boost and vacuum readings are excellent and AFR's look good. yet my fuel economy has gone down quite a bit. where I was averaging around 35 on the highway without a passenger or pulling a trailer I now average around 30/31. I did not have gauges hooked up before so I dont know how it was running, but im wondering what the deal is. bad gas? hot Texas weather?